Px4Flow: Trouble getting any response over I2C

Have you tried setting the parameter to delay boot of the flight controller? This lets the px4flow finish its startup prior to the flight controller setting up the communications. I cant lookup the parameter now, but i can check later.
Setting up the boot delay fixed the startup trouble with the px4flow in my case.

Try setting "BRD_BOOT_DELAY to 10 milliseconds. This helped my problem