Hi guys. Hope someone can help me. Today my Skyhunter did not failsafe after loss in RC i.e. LOW PWM on channel 3. If I did not have FPV the plane would have been lost. I’m attaching my flight data.
I had the following settings:
FS_LONG_ACTN: 1
FS_LONG_TIMEOUT: 10
FS_SHORT_ACTN: 1
FS_SHORT_TIMEOUT: 5
THR_FS_VALUE: 975
Should AFS_ENABLE be 1 to Failsafe on Low RC3 value?
I was flying in FBWA mode when I had no longer control. The plane flied in one direction and then the throttle cut. The plane eventually crashed about 2 km away from the GS.
PS. I’m not able to upload bin file…