Hi
guys,
during last fly i have lost engine and crashed. In the Log my throttle RCIN in RED remain high
and in two time the Rc output engine (GREEN) go down to minimum.
in which case Ardupilot take control of the engine to go down during STABILIZE?
Throttle in stabilize is supposed to be manual pass through from rc channel as far as i know, did it failsafe or something?
Separately why did it cause a crash? Did you try to go back to manual mode when the motor stopped?
Send on-board *.BIN log file of that flight.
the file zip archive is 1.5 mbyte but website continue to show
“Sorry, that file is too big (maximum size is 4.4 MB). Why not upload your large file to a cloud sharing service, then paste the link?”
33 ms near ground… try to controll and in the time i try to find flight mode swich the plane are in the ground