Copter takoff, tilts and crashed, please help me to analyze the log and find the cause

Sorry, I do not have an answer for that. maybe you would like to post it here.

I do not think so. 4*4.2 is 16.8V.

If you have done ESC calibration, frame XY CG check, RC calibration, and motor direction test, probably your motor or ESC is not working properly or you have accidentally configured the ESC to some unknown configurations, for example.

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