I test a new copter. I have the feeling the pixracer board wents mad when using > 4s. Can someone have a look at the Vcc? There is a voltage drop and spikes of the Acc and Mag and Gyro values. It was just a bench test
I test a new copter. I have the feeling the pixracer board wents mad when using > 4s. Can someone have a look at the Vcc? There is a voltage drop and spikes of the Acc and Mag and Gyro values. It was just a bench test