I sent you a PM with my email address. Could you send me the .apj
We have a good relationship with TBS. We should be able to run this to ground pretty quickly.
Thanks’ for sharing your discoveries.
May I ask for the .param file from after your successful first flight?
To be honest I am still a bit scared for the first “overhead” launch. Yes I know, a well tuned ArduPlane can do this easily. But a tuned one?
I just uploaded the AIO that trappy sent me with TBS_LUCID_H7_WING and it worked fine. Orientation is correct with pigtail towards the front and TBS logo on top
The plot thickens! Did you verify that the x and y signals from IMU 1 and IMU 2 are in agreement? I didn’t actually notice the issue until I started trying to arm it, since the artificial horizon was reading correctly (I assume using IMU 1).
How does one download this?
Everything seems to work except the relay randomly stopped working right before take off.
Edit.
It was the vtx. 6s vbat killed the avatar pro. It haopened right when i did a takeoff and canceled. I guess a voltage spike killed the vtx.
Have you flown the chupito few times? The relay fried on my aio. It no longer can toggle them vtx power.
I flew I think about 8 packs before I smashed up my airframe with some dumb (but fun) LoS flying. I didn’t have any issues with my VTX (O4 Pro) during that time, and I was switching the relay on and off (i.e. I didn’t just leave it on).
I have another airframe that I will build out soon, since all the electronics survived. It’s a super fun model to fly.
Any benefits raising the imu fast sampling to 4k or 8k? And the control loop to 400k from 50k? This is a h743 based flight controller. Small Flying wing
For a plane? No I don’t think so.
