Problem landing Gear Tarot TL8X002

Hi. I am using the landing gear Tarot TL96030 with the TL8X002 control board on my drone and when I press switch 9 the train is retracted, but it keeps moving intermittently and does not stay in the final position.

By analyzing the log, it is possible to identify that RCOU.C9 behaved completely inversely to RCIN.C9, is this normal?

I’m using a CUAV V5+ with the CUAV H16 radio with copter 4.0.7.

This is the link to download the log: https://drive.google.com/file/d/1_sUQMg-wq7V5ItX6_Vb0nDIoe8RkdX8M/view?usp=sharing

Hi Jose,

Did you ever get to the bottom of the issue?

Olá Yasin,

I’m using arduino nano between the V5+ and the landing gear controller board.

I’m using the servo library, if you need the code let me know and I’ll share it with you.

Getting to see the same behavior on all these Tarot Landing Gear Boards. Has anyone been able to pinpoint were the issue comes from ?