My apm2.8 crash loiter and althd mode.also when arm in altmd then my quad flip and crash

my quad with apm2.8 and m8n gps.in stabilize mode drone perfectly working ,but when change the althold mode and loiter then its behaving crazy and flip and crash.,plz help.this is my log bellow.

Log File C:\Users\JYOTIRMOY\AppData\Local\Temp\tmpB8E.tmp.log
Size (kb) 851.8515625
No of lines 12960
Duration 0:05:33
Vehicletype ArduCopter
Firmware Version V3.2.1
Firmware Hash 36b405fb
Hardware Type
Free Mem 0
Skipped Lines 0
Test: Autotune = UNKNOWN - No ATUN log data
Test: Brownout = GOOD -
Test: Compass = GOOD - No MAG data, unable to test mag_field interference

Test: Dupe Log Data = GOOD -
Test: Empty = GOOD -
Test: Event/Failsafe = FAIL - ERR found: GPS
Test: GPS = FAIL - Min satellites: 3, Max HDop: 22.27
Test: IMU Mismatch = UNKNOWN - No IMU log data
Test: Motor Balance = UNKNOWN -
Test: NaNs = FAIL - Found NaN in GPS.VZ

Test: OpticalFlow = FAIL - ‘FLOW_FXSCALER’ not found
Test: Parameters = GOOD -
Test: PM = GOOD -
Test: Pitch/Roll = FAIL - Pitch (-64.38, line 12164) > maximum lean angle (45.00)
Test: Thrust = GOOD -
Test: VCC = GOOD -

second log bellow

Log File C:\Users\JYOTIRMOY\AppData\Local\Temp\tmp7EC9.tmp.log
Size (kb) 26.884765625
No of lines 629
Duration 0:00:00
Vehicletype ArduCopter
Firmware Version V3.2.1
Firmware Hash 36b405fb
Hardware Type
Free Mem 0
Skipped Lines 0
Test: Autotune = UNKNOWN - No ATUN log data
Test: Brownout = FAIL - Truncated Log? Ends while armed at altitude 14143504.25m
Test: Compass = GOOD - No MAG data, unable to test mag_field interference

Test: Dupe Log Data = GOOD -
Test: Empty = FAIL - Empty log? Throttle never above 20%
Test: Event/Failsafe = GOOD -
Test: GPS = FAIL - Min satellites: 0, Max HDop: 99.99
Test: IMU Mismatch = UNKNOWN - No IMU log data
Test: Motor Balance = UNKNOWN -
Test: NaNs = GOOD -
Test: OpticalFlow = FAIL - ‘FLOW_FXSCALER’ not found
Test: Parameters = GOOD -
Test: PM = UNKNOWN - No PM log data
Test: Pitch/Roll = GOOD -
Test: Thrust = GOOD -
Test: VCC = GOOD -

The thing that jumps out at me is the GPS errors. I’d wager you do not have the GPS connected to the proper port on that APM 2.8. Post some pictures of how you have ever thing connected to the APM.

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i already use same way to connect gps.and working good previously.but now not working and crash my quad …