Full throttle spike after transitioning from QHOVER to FBWA

Hello!
We were testing quadplane on the stand to see servo and motors behavior and we noticed that after transition there is a full throttle spikes. I’ve added screenshot from logs. RC9 - tilt-rotor servo. RC6 - motor.
Do you know what could it be and how to fix it?
also, log file is attached.
https://drive.google.com/file/d/1XJSVL4rEl7eJm1hYQqnmimFstyOVcV9G/view?usp=sharing

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