When calibrating the compass, compass one has low numbers but compass 2 has very high last number. It flies good but seems to be twitchy on yaw? Ran auto log analyzer and this is the results.
Log File C:/11292014.log
Size (kb) 4666.240234375
No of lines 61837
Duration 0:04:16
Vehicletype ArduCopter
Firmware Version V3.2
Firmware Hash c8e0f3e1
Hardware Type
Free Mem 0
Skipped Lines 0
Test: Autotune = UNKNOWN - No ATUN log data
Test: Balance/Twist = GOOD -
Test: Brownout = FAIL - Truncated Log? Ends while armed at altitude 3.97m
Test: Compass = FAIL - Large compass off params (X:-92.00, Y:-8.00, Z:-172.00)
Large compass offset in MAG data:
Z: -172.00
Large change in mag_field (87.75%)
Max mag field length (553.74) > recommended (550.00)
Test: Dupe Log Data = GOOD -
Test: Empty = GOOD -
Test: Event/Failsafe = GOOD -
Test: GPS = GOOD -
Test: IMU Mismatch = GOOD - (Mismatch: 0.18, WARN: 0.75, FAIL: 1.50)
Test: Parameters = GOOD -
Test: PM = GOOD -
Test: Pitch/Roll = GOOD -
Test: Thrust = GOOD -
Test: VCC = GOOD -